Current article

Dewater Sinking Analysis of North Anchorage Caisson for the Fourth Nanjing Yangtze River Bridge


MU Bao gang,ZHU Jian min,GONG Wei ming and NIU Ya zhou

DOI:10.11835/j.issn.1674-4764.2010.05.025

Received March 15, 2010,Revised , Accepted , Available online July 01, 2015

Volume ,2010,Pages 135-141

  • Abstract
Combined with construction of north anchorage caisson, field pumping tests were carried out. Permeability coefficient was acquired for dewater sinking. Water yield of single well and total water inflow of caisson excavation were calculated. It is found that the measured amount of total water inflow is slightly larger than the theoretical value. Based on effective stress principle, the compression of phreatic water aquifer caused by dewater is almost negligible,and the ground settlement is mainly composed of confined water aquifer compression. The calculated settlement curve along the levee was in good agreement with the measured data.